Turns out one of the metering blocks wasn't drilled properly. There is still a slight tuning issue which it's going back on Saturday for. I suspect the floats are set too high and the carb is flooding on reasonably heavy acceleration, it loses power and bogs down but goes well once cleared out.
The car physically drives really really nice, and it's nice having something with a bit of power again. I doubt it's making the power I hoped for but I'll reserve my "opinions" untill I get a set of headers and better air cleaner on it, and get it fully broken in. The exhaust sounds a little harsh since the rebuild, I suspect from the increased compression, cam and current state of tune. It is a true dual exhaust without an "H" or "X" pipe. We'll see what it sounds like with headers and depending might get an X pipe at the same time to mellow it out.
It also turns out I wasn't getting full throttle on the carb, it wasn't engaging the kickdown. I made up this little bracket to alleviate that problem. I painted it with Tamiya PS-52
So far so good......
Also, here's the first outing with the car.....